So it was arranged a week ago, "we'll make it Wedensday" and once again like clock work Ray walks down the driveway with an arm full of "spare parts and man-cave treasures" right on 7.30am to begin turning some spanners on Monty.
The timing cover and gasket was to come off and a new gasket installed to stop a small oil leak which I had cleaned up the week before in preperation for today and this picture below shows what it was like after I removed the radiator and also over the past 12 months I have degreased and pressure washed down in here a good few times before so it was rather dirty and covered in greasey crap to begin with.
Also while we were at it and the radiator was out of the car it was decided that the water pump come off also as there was a 3mm bit of forward and back movement on the water pump impeller shaft when you pulled the fan in and out, fix it now and fix it right, but the first thing to do was remove the lower pulley...
Then the water pump came off by unbolting 4 x bolts with all seemed in good condition..
Clean as a new one
Next we were off to dad's factory to use the big press to press out and remove the water pump impeller shaft but this is where things got off track for the day. We cracked and broke the water pump housing as it twisted just so slightly in the press and some of the casting broke off.. #%*@ - anyway not to worry as Ray said he has about 6 others at home to replace it with and will take it back there to do the repair on and fix the front and back movement of the shaft.
The end result - Fantastic!
After lunch the radiator went back in the car with 2 x new mounting bolts and then we spent a good hour I would say adjusting and measuring the bonnet and also the radiator to get the bonnet sitting just nice, a little tweaking here and there and soon we were both happy with the look of it considering that no bonnet latchers are installed to hold it all down nice a tight, but they will come soon..
A great day it was, with great conversation and a few good laughs along the way and once again Ray thanks so much for your time and effort...
Ray emailed me tonight and has repaired/replaced the water pump housing and that after stripping the broken pump down has discovered it was a previously botched up, dodgy repair of about 50 years ago probably...
We were both surprised when it broke in the press today, but more so Ray who has pressed out many of these before and never had one let go on him in this fashion.
This is some of what Ray wrote in his email:
- 1. Changed housing (pressed 2 at home the same way no problem, so may have been cracked already)
- 2. Changed Impeller (Monty's was corroded on the inside)
- 3. Replaced Shaft (Monty's was corroded and bent)
- 4. Replaced Fan Belt Pulley (Monty's was a bit warped)
- 5. Replaced Fan Blade Hub ( Monty's was a bit loose once the rust let go, that would have been fun down the track)
- 6. Replaced front and rear thrust washers
- 7. Fitted New Internal Baffle (Monty's had hole)
- The main bush (Stripped out gland packing and replaced)
- The front bush (Not drilled for lube, would have failed. Drilled and reamed)
Good days fun, another few baby steps.
Love it Grant. Keep the updates coming!
ReplyDeleteI think Monty has more character in Black and White.
ReplyDeleteMonty is looking good, very good! Really enjoying following the restoration!
ReplyDeleteLove your blog! I've been doing a lot of research into gasket material and this has really helped. Thank you!
ReplyDeleteThis is really a nice and informative, containing all information and also has a great impact on the new technology. Thanks for sharing it water extraction
ReplyDelete